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UPDATED INFO How I did it - Poorboy Conversion for 82 GL1100

109919 Views 285 Replies 61 Participants Last post by  CrystalPistol
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This is not originally my idea, I have seen Alternators grafted onto many different vehicles over the years.

I was not happy with the limited electrical power of the stock charging system of my 82 GL1100 Aspencade. When I realized the limitations of the GL1100 charging system I went looking for ideas. I did a little searching of the internet for info, I found several references to the “poorboy” kit. I wanted to know what it looked like so that I might be able to build my own. At the time I just gathered the info I needed to build what I thought might work without keeping track of where I got the info or who’s idea it was. After all I was only going to build the one for myself.
(edited)Don “Poorboy” Pigott came up with a kit that fit the GL1200 , this kit does not work with the GL1100. Some of the info I got was from Dan Filipi over at Naked Goldwings.com , who did this to his 83 GL1100. My thanks go out to these two men for their pioneering efforts.


It took me many hours to come up with solutions to MANY little issues. If you do this conversion yourself,even following my method you will see what I mean. This is a guide to do it yourself NOT a guaranteed Step by Step (insert legal disclaimer here).



Is it worth it? You bet it is ,I have more electrical power than I can use now. Like running the heated vest,grips,stereo,highbeam headlight,two 50 watt driving lights,two 55 watt ditch lights,cig lighter,trailer with electric cooler ALL AT THE SAME TIME!!!!

This conversion is designed to use a specific alternator,others may work. I found mine at the auto wreckers after opening several hundred hoods. The winner is a Nippondenso unit from a 1988 Pontiac Firefly Turbo 1.0 liter .



It measures 130mm or 5-1/8" from front of pulley to the rear of the unit and100mm or 4" in diameter. On the bottom of the unit the rear mounting foot is a stamped steel unit that can easily be unbolted and discarded.



No cutting required like the Geo Metro Alternator. I paid $25 and had a shop rebuild it forabout $100 he even painted it satin black before assembling it ,cheaper than one from the auto parts store.



Step one: strip the bike to this level



Engine Auto part Automotive engine part Fuel line Vehicle






Pull the timing covers off and remove the crank bolt.
Grind the grade stamp off the head of the bolt.
Chuck the crank bolt in a 1/2" drill press,spin it fast to find the center by holding a 1/8" drill bit.
Your not trying to drill the bolt yet just make a mark so you can turn it overand center punch the mark.
Now use a 1/4" bit and drill the center punch mark about 3/4" deep.Make sure the bolt is square and plumb to the bit .
Reinstall the crank bolt,reinstall the timing covers with rubber gaskets,but make a notch in the rubber where it passes over the crank bolt.
This is where you will put the pilot bit of the hole saw in the next step,you may have to remove a little of the aluminum as well.The pilot bit needs to turn freely in the hole you drilled in the end of the crank bolt and NOT catch on the timing covers at all.They will shift if it catches(ask me how I know)




Auto part






Use a 1 3/8" bimetal hole saw to cut a hole in the timing covers,medium speed light pressure works for me.use cutting fluid if you have it.





Auto part Engine Motor vehicle Vehicle Fuel line






showing the 1-3/8" hole for the new pulley perfectly centered over the end of the crank.

Notice the rubber gasket is split and pulled back out of the way for now.

That should be enough work to reward your self with a nice frosty beverage.

Now remove the covers and CLEAN up the mess you made. Metal chips (even aluminum)aren't good for the belts.Remove the drilled crank bolt and save it for when you help your buddy do his conversion.
You will need to get a longer bolt to hold the new pulley .Same thread pitch but 55mm or 60mm long. I got mine free from the local Honda dealer.
I was going to use the following drawing to have one made, but my machinist was too busy and I couldnt wait .

Text Diagram Font Line Parallel

I used a 2" pulley from another scrap alternator and bushed the center hole down to fit the 12mm X 60mm bolt.giving me a 1 to 1 drive ratio .
I would have prefered to use a 3-1/2" drive pulley but couldnt find one in time. 1 to 1 works fine but doesnt charge well under 1200RPM. I get 13.5 volts at 1300RPM.

Auto part Wheel Machine tool Automotive wheel system Rim




Here's how mine looks installed, hole in timing cover is 1.375",spacer behind pulley is 1.360"diameter.
Nice close fit to help keep the road crap out.I opened my timing covers the other day to checkfor debris,Im happy to say that after 3500km./2300miles everything is clean as a whistle in there.



Now thepart that took me the longest to get just right. when you strip the bike down to start this build you will come across the top motor mounts behind the tin heat shield in front of the carbs .
You want the left one to use as a pattern,dont forget to make the "dowels" in the new piece. Materials list: about 8 inches of 3 X 1/4 inch flat bar stock about 2 inches of 9/16 inch tube for dowels. I used a Zip disc to cut mine out





Here's the pattern











Drawing






That's 5/8" up and 1-3/8" over.





time for a frosty beverage here





now its time to fit things up and butcher the tin.

New motor mount first then the heat shield tin.

Auto part


For the pivot bolt I used a 10mm X about 3-1/2". 3/8 will work but the 10mm bolt is a better fit. Iused the pivot bolt from the car I took the alternator from.
Weld bolt head to new bracket,use a spacer and nut to pull the bolt tight and square to the bracket once you establish the proper length bolt. Do not use "Allthread" rod except for the mock up stage.
Adjust spacer length so that crank pulley and Alternator pulley are perfectly in line





Auto part Automotive engine part Engine






another view showing clearance to the carbs





Engine Auto part Fuel line Vehicle Automotive engine part











time to butcher the tin,go slow and take little bits.The alternator needs to move a fair bit so have your belt handy,I used a Dayco Polycog #5030280 . Cut just enough tin away to allow the belt to be rolled onto the pulley.Mine could have been cut less

























Dont forget to unplug the voltage regulator,this can be plugged back in to use the stock system in case of an Alternator failure/belt breakage in the middle of nowhere.





Another frosty beverage perhaps?





More tin to cut













The fan shroud needs to be trimmed. To position the rad properly I spaced the bottom out 3/4".Longer bolts needed here.Use the same rad hose but rotate it slightly to get the best fit,leave hoses off for now.











Now the part that takes a bit of fiddling...........





Modifying the fan motor support requires removing the rad andfan blade and fanmotor several times next photo shows the angle bracket I welded in after cutting out the support at the 8 o'clock position.Not the new bracket fits behind the new belt and uses the stock mounting bolt holes.











nextbit of butchering......





I had to trim theleading edge of the fan itself a little the next photo shows how much I removed to clear the new belt. I cut them off using tin snips and smoothed them with sand paper.











there seems to be no adverse effectson the ability of the fan to cool the engine. last bit of butchering to do..... The lower fairing mounts need to be cut like this and then reversed left for right because you have moved the rad bottom out 3/4". This mod solves that problem.











trim them both to look like the one on the right of the photo.File smooth and paint black.





installed they should look like this











And this







Once you put it all back together you will notice that you dont have to modify the plastic at all.It does touch the alternator but only just.





Wiring is simple There are only 2 wires I used,heavyguage from alternator output to inline blade type fuseholder and then to battery positive. I have a 40 amp fuse in mine so far it hasnt ever blown. Of the 2 wires coming out of the green plug in on the back of the alternator I used the one marked " I " or " IGN " to the ACC terminal on the fuse panel. Check your work and fire it up . You should have 13.5 volts just above idle and 14.5 above 2500RPM You now have 55amps of power to run LOTS of stuff.





Feel free to use this info for yourself or to help out a friend.

If you make some money off of it dont forget where you learned it from and make a donation to this forum.

If you make a lot of money find me.....

Enjoy, Todd

Any questions?

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Some pics as I'm waiting on parts to complete water pump. The before pic and a couple of the upper mount. I had to notch it in as it rocked back and forth over the coaming.
Some updated pics. I got the water pump replaced and the hardware on for the alternator, now I'm doing the wiring. Note the rag I left on the coolant gooseneck on top of engine and I rearranged the lower gooseneck (and it's just finger tight) to keep stuff out of the lower part.
Once I get all that I'll refill all fluids and crank it up.

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Some updated pics. I got the water pump replaced and the hardware on for the alternator, now I'm doing the wiring. Note the rag I left on the coolant gooseneck on top of engine and I rearranged the lower gooseneck (and it's just finger tight) to keep stuff out of the lower part.
Once I get all that I'll refill all fluids and crank it up.
Oh yeah, just realized, haven't tackled radiator yet. That's next, then finish wiring...
What does that crank pulley come from?
I like it and the serpentine drive.
What does that crank pulley come from?
I like it and the serpentine drive.
That's the one that comes with Don's kit, I got it from him. I got the alternator (Remy 14946), belt (Gates K030310) and wiring local.

It all fit like it's supposed to be there.
Cool!
Nice Job!
Spent most of yesterday trying to fit the radiator back on. I tired tilting the fan, moving it as close to the radiator as possible, cut the 8 o'clock leg, trimmed the shroud. The lower pulley cleared with no problem. The upper run of the belt would only clear the fan mount by only 1/4 inch no matter how much I moved the fan or radiator in or out. I ordered a fan online to install on outside of radiator.
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You're not the first I've heard that had issues, but I don't know why you'd throw in the towel. An "outside" the radiator fan will introduce its own set of problems. Unless it's quite thin, you might contact it with the front wheel. Ungood.

I had to pull my fan back out and do additional trimming. In addition to the leg, I had to enlarge the notch that Mother Honda already had in there. A flashlight worked wonders for me to see where the interference was. And, yes, I used Don's kit.

<< EDIT: Ok, I'm an idiot. Forget everything I said. Yours is an '82 and a bit more challenging. >>

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Just going to try the outside fan to see if the fit is better; it is a thin mount fan and was only $25.
I still have the oem fan so if the outside one doesn't work I'll work with the oem more to a fit I'm satisfied with.
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I finally got the fan and installed. There's plenty of room between the fender and fan. The clearance in one of the photos looks close but it's just the angle, there's plenty room as you can see in the other photo. I like this location rather than the cut up assembly, close fitting on the inside of the radiator.
I wrapped up all the mechanical, refilled fluids and ran it till hot. The fan worked as it should.
I measured 12.8 at the battery at 1000 rpm, 14.4 above 2000 rpm.
I'm still fitting all the plastic, just requires small adjustments around the bottom of the radiator, around the alternator and trim a bunch off the lower cowl cover (the black panel that used to fit around the carb but won't now since the alternator is there).

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Have you fully compressed the front-end to make sure of ...you know what?
Have you fully compressed the front-end to make sure of ...you know what?
Yeah did that. A lot tougher since I rebuilt the forks but I got it to compress, with help. The bottom of the plastic fender makes contact but only that, not enough to move the fender. I will test going in and out of driveway when the weather permits. My drive has a tall curb where it meets the street. Maybe one of these days I'll get it re-done to where it's smooth pulling in and out.

I didn't remove the protectant grill on the front of the radiator and I put extra 1/4" spacers behind the spacer mounts I got from Don so I have so room to take if necessary.
Right on. Looks great!
:thumbup:
Yeah did that. A lot tougher since I rebuilt the forks but I got it to compress, with help. The bottom of the plastic fender makes contact but only that, not enough to move the fender. I will test going in and out of driveway when the weather permits. My drive has a tall curb where it meets the street. Maybe one of these days I'll get it re-done to where it's smooth pulling in and out.

I didn't remove the protectant grill on the front of the radiator and I put extra 1/4" spacers behind the spacer mounts I got from Don so I have so room to take if necessary.
I could not gain enough room to get clearance I was satisfied with so I went with a 7" fan. I took the 1/4" spacers out, trimmed 1/8" off the spacers that came in the kit (which allowed them to screw on up to the threads on the original mounts) and I also trimmed the radiator front grate so the fan would sit against the radiator fins. The stock radiator was too narrow to get the 10" fan to sit against the fins. I put on a ratchet strap on each fork and ratcheted down to the stops and had clearance that I was satisfied with so I'm now done. Refilled everything and optest sat. 20 months later, after all the work it's done. Now to work on improvements. I think the stereo and speakers are first.

I found an interesting thing about the electric fans as I test ran them to ensure I was hooking up the correct polarity and for airflow, they ran more efficient when I flipped the fan blade assembly over.
Wow, I sure do enjoy this forum! So much talent and courage to work outside the box to make our bikes better! RoadRogue, your project here is just one inspiring example!

I am coming to this project REALLY late, and expect you have many miles on the bike now. Some of us would like to hear of any maintenance issues with this system. Truthfully, I can't see any cause for any. Well, almost.

It made me nervous to see that lower radiator hose kicked over that 3/4" from straight on. Looks like the nipples it connects to were straining the hose over the edges of the nipples. Not a problem with a fresh, new, supple hose, but over time I could see a problem. I was wondering if this has been a problem at all?

Ever considered machining a spacer to go under that t-stat cap to space the cap out the 3/4" that the radiator moved? It wouldn't affect anything except to re-align the nipples so the hose isn't strained at all.

This is a great project and you did a great job of documenting it. Thanks!
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I could not gain enough room to get clearance I was satisfied with so I went with a 7" fan. I took the 1/4" spacers out, trimmed 1/8" off the spacers that came in the kit (which allowed them to screw on up to the threads on the original mounts) and I also trimmed the radiator front grate so the fan would sit against the radiator fins. The stock radiator was too narrow to get the 10" fan to sit against the fins. I put on a ratchet strap on each fork and ratcheted down to the stops and had clearance that I was satisfied with so I'm now done. Refilled everything and optest sat. 20 months later, after all the work it's done. Now to work on improvements. I think the stereo and speakers are first.

I found an interesting thing about the electric fans as I test ran them to ensure I was hooking up the correct polarity and for airflow, they ran more efficient when I flipped the fan blade assembly over.
Some pics showing how the alternator looks in the panel, dropped the front fender a quarter inch and the fan.

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in the conversion kit do you know what the alternator was suppose to fit in a car ?? reason asking I done the conversion on my 83 aspy and I picked up the steel for around 10 bucks and the alternator I used was used on a 91 Pontiac it had a built in regulator so my radiator only had to be moved out a 1/2 inch and the driven on the crank I used a alternator pully off a 84 ford truck the smog pump belt was same just had to turn the back groove off
nice deal steve! got some info on the pulley? looks like the radiator is all original setup?
to the guys that are using this conversion to lessen the room from the crank to radiator and the metal on the lower faring I used a 1988 chevy sprint it has a small v-belt pulley and for the crank pulley I used a alternator pulley off a 1985 ford truck which has the same v-belt groove
Hi All, I have a question, why is everyone using alternators that are so old ? Is it because they are getting them from the scrap yard or is there another reason ? Do the attaching wings need to be clocked at a certain angle ? Do the pulleys need a certain belt or whatever fits the pulley. I want to attach an alternator to my 1982 GL1100 and I would like some info if possible. Thank You, John.
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